The following is a review of the MicroHeli Precision Tail Rotor
The first part of this review will center around the build quality of the
Precision Tail Rotor.
Initially some good close up photos of the Tail Rotor to give you a feel
for the CNC quality.
Now, anybody who has paid any attention to the media (including this site)
will be aware that the early Precision Tail Rotors were shipped with incorrect
washers retaining the blade grips, this was an assembly error at manufacture,
steel washers were specified in the design. There may still be some of
these faulty tail rotors in circulation. Before installing and using the
tail rotor check that the washers holding the blade grips to the central
hub are either brass or steel, if they are aluminium they are not capable
of sustaining the centrifugal forces acting on the tail rotor and you will
get a blade grip failure. Please contact support@microheli.com to obtain new washers (if you find your washers to be made of aluminium).
An easy check is to use a magnet, aluminium is unaffected by magnetic forces.
If in any doubt please see the announcement on the front page of the MicroHeli website.
OK, public warning service out of the way, on with the review.
The tail rotor is nicely engineered and has a quality feel both in the
finish and the smoothness in the bearings. The CNC machining is very nice
indeed and the whole unit has a solid feel about it. There is very little
slop or play in the unit as a whole. Those are the positives in terms of
build. The tail rotor also comes with a new shaft, however, to use this
the tail belt gear would need to be glued/loctited to the shaft in a similar
fashion to a motor pinion as the supplied shaft has no splines.
On the negative side, the tail blades are held on using an 'M2' bolt and
nut, whilst this is perfectly adequate I would have preferred to have seen
a nyloc nut, in this case some loctite is a necessity. In most cases the
forces acting on the screw will try to keep it in place rather than throw
it out but I wouldn't want the nut coming off at high speed!
Secondly the blade grips themselves are held on with an #0 bolt and washer,
personally I would have preferred an 'M2' in this position. To be clear
the #0 can quite adequately deal with the forces placed upon it in this
application but an 'M2' would be much more conservatively within it's loading
limits. Before installation of the new tail rotor I would recommend just
checking the #0 blade grip bolts for loctite, it is good practice to check
this kind of thing on ready assembled goods.
Addendum: Having discussed this with MicroHeli they have changed the blade
grip bolts on new Precision Tail Rotors to be an 'M2'. The reason was that
if a washer were to fail the cap head on an 'M2' would not pass through
the bearing like the #0, so it is an extra safety precaution. I have a
new tail rotor to review but I can't review this change currently as my
review model has the #0 bolts.
I removed my old tail rotor hub and directly replaced it with the MicroHeli
unit. This is a one for one swap and the MicroHeli hub is correctly sized
to fit onto the stock tail shaft. So no need to use the free supplied one,
although the supplied one is slightly longer (which would allow for more
pitch throw on the tail).
Below is the initial mounting picture ....
Having attached the unit to the hub the retaining grub screw can be loctited
and tightened and the ball links popped onto the blade grip balls. In terms
of build that is all there is to it.
Initial Flight Testing
My inital hover tests showed that this tail is certainly behaving differently
to the stock Align unit. The gyro settings were immediately noticeable
as not being correctly set for this tail. The weather wasn't being particularly
kind and trying to setup the gyro in 10mph winds isn't something I would
advise to the feint hearted. I settled for setting up non heading hold
mode as the Align gyro is known to be a little bit more difficult to get
going properly on HH mode.
Having set the gain for non heading hold things settled down quite a bit
and I was able to get a feel for the new tail response. Initial thoughts
were that the overall power of the tail was exactly the same as the stock
unit, which is unsuprising given that the pitch change mechanism is unchanged
by this upgrade. The ability of the tail to respond to very minor stick
movements was more aparent and the tail had an overall more refined feel
to it. I had noticed on the ground that even tiny stick movements were
equating to an adjustment in the tail blade pitch which is normally lost
in the slop on the stock unit.
My initial thoughts are that this upgrade has brought a more refined and
precise tail response but given the weather conditions I would want for
calmer weather to experiment with some more advanced moves than just hovering.
I'll be doing some more advanced flight testing and then subjecting the
tail to some more extreme forces on my bench test, hopefully the tail will
stand up to this type of testing now that it has the brass washers fitted.
Hovering and Circuits
Since my inital flight tests I have had some problems with getting HH mode
to work without tail wag. This turned out to be the fact that the MicroHeli
balls on the tail blade grips are slightly larger than Align balls. This
means the ball links are a little stiff and introduces tail wag. I remedied
this by giving each ball link a firm squeeze with some pliers whilst it
was still on the ball. A few minutes later and all was freed up and tail
wag was gone.
I also changed to a CSM SL420 micro gyro to get a better gain setting and
locked on hold. This I certainly achieved. Having ironed out all the issues
I reduced the yaw rates and set about having a proper feel of the tail
response. Certainly my inital observations of a more precise response for
very small stick movements is in evidence. For larger movements the tail
feels exactly like the stock unit.
To get a true comparison I will switch between tail hubs on my next flights
to see how the tail response changes. For the moment I'm happy in that
the tail is performing perfectly with rock solid heading hold and perfect
stops with no bounce on short sharp stick movements. Of course this could
just be the gyro, only continually swaping the stock and upgrade hub will
give me the information I need to draw final conclusions.
More on the hub swapping later, now for some stress testing.
Stress Testing
In order to properly test the overall stress that this tail rotor can take
I needed to make it's job that much more difficult. The easy answer to
this is headspeed. So armed with a totally inappropriate pinion and a nice
powerful motor I set about upping the headspeed to really place some stress
on the tail rotor system. I topped out at 2850 RPM on the head, any faster
was going to cause some vibration problems plus sitting next to the thing
going at that speed wasn't all that comfortable.
Once at full throttle I tried large tail rotor pitch changes to load it
up. The tail coped perfectly well with this abuse. The only permanent damage
being to my nerves. A close inspection of the tail post stress test revealed
no evidence of imminent failure or fatigue. Based on this I think it can
cope adequately with the most agressive flyers 3D moves.
Final Thoughts
I've taken a long time to come to the conclusions on this test. The tail
on the T-Rex is an interesting piece of engineering. In stock form it appears
to be sloppy but when run up to speed and matched to a good servo and gyro
this is hidden by those same components. Unfortunately, matched to a poor
servo or gyro the dreaded tail wag appears. This meant having to spend
some time working out what was actually performance being facilitated by
the MH tail rotor and what was just a good gyro and servo making up for
the inadequacies of the stock tail. After various flights trying different
flying styles it was quite by accident that the conclusion of this test
came about. I was trying to iron out the problems of running governor mode
on the 400DH and suffering tail wag due to the motor surging. It was during
this problem that I did a hub change to the MH tail and suddenly the difference
was quite apparent. The gyro and servo matched to the stock tail was realy
struggling to keep the tail together through the oscillating motor RPM,
making the tail wag and kick with each oscillation. With the MH tail fitted
this problem reduced, it was still there but you could see the difference,
the servo and gyro were coping much better. This might seem like an odd
way to end the test but for me it proved the point. There must have been
a performance improvement as the MH tail is such a solid and slop free
system, finding the level of that increased performance just required a
slightly unorthodox approach.
Before you decide to buy the MH tail rotor in order to fix that tail wag
problem I would caution you to stop and think. A large number of the tail
wag issues are down to the mechanical setup of the tail, a cheap gyro or
a slow servo. If you are confident that these issues are not a part of
your problem then changing to the MH tail will give you a more locked in
tail response and 'possibly' get rid of that wag. A far better reason to
buy this tail is to get a better and more precise responding tail rotor
as that is the focus of this component. It is entirely possible that if
your tail wag issues are mechanical then installing the MH tail could make
it worse as all those nasty imperfections in your linkage system will be
translated directly into tail pitch changes rather than being lost in the
slop of the stock unit.
If you have this component rate it using the TRexTuning rating system ......